谢荣团, 朱阳阳. 20 MW水轮发电机纵差保护动作原因分析及处理[J]. 内蒙古电力技术, 2018, 36(2): 39-42. DOI: 10.3969/j.issn.1008-6218.2018.02.012
引用本文: 谢荣团, 朱阳阳. 20 MW水轮发电机纵差保护动作原因分析及处理[J]. 内蒙古电力技术, 2018, 36(2): 39-42. DOI: 10.3969/j.issn.1008-6218.2018.02.012
XIE Rongtuan, ZHU Yangyang. Cause Analysis of Longitudinal Differential Protection Operation of 20 MW Hydrogenerator and Its Processing[J]. Inner Mongolia Electric Power, 2018, 36(2): 39-42. DOI: 10.3969/j.issn.1008-6218.2018.02.012
Citation: XIE Rongtuan, ZHU Yangyang. Cause Analysis of Longitudinal Differential Protection Operation of 20 MW Hydrogenerator and Its Processing[J]. Inner Mongolia Electric Power, 2018, 36(2): 39-42. DOI: 10.3969/j.issn.1008-6218.2018.02.012

20 MW水轮发电机纵差保护动作原因分析及处理

Cause Analysis of Longitudinal Differential Protection Operation of 20 MW Hydrogenerator and Its Processing

  • 摘要: 针对龙口水电站20 MW发电机纵差保护动作事故,对发电机电气一次设备进行绝缘电阻测试并分析事故动作报告,确定事故原因为发电机励磁变压器高压侧电缆冷缩终端头V相绝缘击穿并对地放电。将励磁变压器高压侧电缆冷缩终端头更换为热缩终端头,并针对发电机纵差保护动作未启动PLC电气事故停机流程的问题,在发电机监控系统PLC电气事故停机流程中增加了SOE量启动源。处理后,发电机运行状况良好。

     

    Abstract: To the longitudinal differential protection operation accident of 20 MW hydrogenerator at Longkou Hydropower Station, confirm the cause of the accident is the V-phase insulation breakdown of the cold-shrinkable terminal head on the high-voltage side of the hydrogenerator excitation transformer after the test of insulation resistance of the hydrogenerator electrical primary equipment and the analysis of accident action report. Replacing the cold-shrink terminal of the high-voltage side of the excitation transformer with a thermal shrink terminal, and increasing the SOE startup source in the PLC electrical shutdown process of the hydrogenerator monitoring system. After processing, the hydrogenerator runs in a good condition.

     

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