严寒夕. 1050 MW超超临界机组初压/限压切换过程中扰动原因分析及解决措施[J]. 内蒙古电力技术, 2019, 37(4): 91-93, 96. DOI: 10.3969/j.issn.1008-6218.2019.04.013
引用本文: 严寒夕. 1050 MW超超临界机组初压/限压切换过程中扰动原因分析及解决措施[J]. 内蒙古电力技术, 2019, 37(4): 91-93, 96. DOI: 10.3969/j.issn.1008-6218.2019.04.013
YAN Hanxi. Analysis of Load Fluctuation in Steam Turbine Switching Process from Initial Pressure to Limit Pressure of 1050 MW Ultra Super Critical Unit[J]. Inner Mongolia Electric Power, 2019, 37(4): 91-93, 96. DOI: 10.3969/j.issn.1008-6218.2019.04.013
Citation: YAN Hanxi. Analysis of Load Fluctuation in Steam Turbine Switching Process from Initial Pressure to Limit Pressure of 1050 MW Ultra Super Critical Unit[J]. Inner Mongolia Electric Power, 2019, 37(4): 91-93, 96. DOI: 10.3969/j.issn.1008-6218.2019.04.013

1050 MW超超临界机组初压/限压切换过程中扰动原因分析及解决措施

Analysis of Load Fluctuation in Steam Turbine Switching Process from Initial Pressure to Limit Pressure of 1050 MW Ultra Super Critical Unit

  • 摘要: 某火电厂汽轮机在初压/限压切换过程中出现负荷瞬时上升问题。从初压/限压切换的逻辑及切换过程中主要参数的变化分析,确定原因为压力控制器指令上升瞬间和转速负荷控制器指令下降瞬间有短暂的时间间隔,造成高压调节阀指令上升,调节阀开度瞬间达到80%,导致负荷波动。在对压力控制器逻辑中延时块进行更改后,初压/限压切换过程中高中压调节阀平稳无动作。

     

    Abstract: Instantaneous rise of load during the initial pressure/limit pressure switching process of a steam turbine occurs in a thermal power plant. From the logic of the initial pressure/limit pressure switching and the change of the main parameters during the switching process, the reason is that the pressure controller command rises moment and the speed load controller command decreases moment, and there is a time interval of about 1 s, causing the high pressure regulating valve command to rise. The opening of the regulating valve reaches 80% instantaneously, causing load fluctuations. After the delay block in the pressure controller logic is changed, the high pressure regulating valve is stable during the switching process.

     

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