余兴刚, 魏海峰, 朱太春, 郭绪宏, 蒋伯华. 1000MW机组给水泵汽轮机轴封系统故障分析及处理[J]. 湖南电力, 2022, 42(5): 119-122.
引用本文: 余兴刚, 魏海峰, 朱太春, 郭绪宏, 蒋伯华. 1000MW机组给水泵汽轮机轴封系统故障分析及处理[J]. 湖南电力, 2022, 42(5): 119-122.
YU Xing-gang, WEI Hai-feng, ZHU Tai-chun, GUO Xu-hong, JIANG Bo-hua. Fault Analysis and Management of Feedwater Pump Turbine Shaft Sealing System for a 1000MW Unit[J]. Hunan Electric Power, 2022, 42(5): 119-122.
Citation: YU Xing-gang, WEI Hai-feng, ZHU Tai-chun, GUO Xu-hong, JIANG Bo-hua. Fault Analysis and Management of Feedwater Pump Turbine Shaft Sealing System for a 1000MW Unit[J]. Hunan Electric Power, 2022, 42(5): 119-122.

1000MW机组给水泵汽轮机轴封系统故障分析及处理

Fault Analysis and Management of Feedwater Pump Turbine Shaft Sealing System for a 1000MW Unit

  • 摘要: 某新建燃煤电厂1 000 MW机组采用1台100%锅炉最大连续出力容量的汽动给水泵,调试期间该机组给水泵汽轮机轴封系统出现轴封蒸汽带水和给水泵侧轴封管道异响的故障。通过调整与分析,发现造成上述故障的原因为轴封回汽管道安装方式设计不合理和凝汽器内轴封蒸汽管道套管安装不完善。采取在轴封回汽管道最低点处加装疏水水封筒、在凝汽器内轴封蒸汽管道上加装保温的措施,成功排除了给水泵汽轮机轴封系统的故障。

     

    Abstract: A 1 000 MW unit in a newly-built coal-fired power plant adopts a steam-driven feed water pump with a capacity of 100% boiler maximum continuous rating. During commissioning, the shaft seal system of the feed water pump turbine of this unit has the faults of water entrainment of shaft seal steam and abnormal noise of the shaft seal pipe at the side of the feed water pump. Through adjustment and analysis, it is found that the causes of the above-mentioned failures are unreasonable design of shaft seal steam return pipe and imperfect installation of shaft seal steam pipe sleeve in condenser. The fault of shaft seal system of feed water pump turbine has been successfully solved by installing hydrophobic water seal cylinder at the lowest point of shaft seal steam return pipeline and installing heat insulation on shaft seal steam pipeline in condenser.

     

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