秦刚华, 汪黎东, 汤光华, 苗丰, 刘洁, 陈彪, 黄斐鹏. 燃煤电厂脱硝催化剂调整策略研究与应用[J]. 电力科技与环保, 2021, 37(1): 47-51.
引用本文: 秦刚华, 汪黎东, 汤光华, 苗丰, 刘洁, 陈彪, 黄斐鹏. 燃煤电厂脱硝催化剂调整策略研究与应用[J]. 电力科技与环保, 2021, 37(1): 47-51.
QIN Gang-hua, WANG Li-dong, TANG Guang-hua, MIAO Feng, LIU Jie, CHEN Biao, HUANG Fei-peng. Research and application of adjustment strategy of denitration catalyst in coal-fired power plant[J]. Electric Power Technology and Environmental Protection, 2021, 37(1): 47-51.
Citation: QIN Gang-hua, WANG Li-dong, TANG Guang-hua, MIAO Feng, LIU Jie, CHEN Biao, HUANG Fei-peng. Research and application of adjustment strategy of denitration catalyst in coal-fired power plant[J]. Electric Power Technology and Environmental Protection, 2021, 37(1): 47-51.

燃煤电厂脱硝催化剂调整策略研究与应用

Research and application of adjustment strategy of denitration catalyst in coal-fired power plant

  • 摘要: 自国内各类燃煤机组完成超低排放改造,脱硝催化剂大面积进入寿命末期,电厂管理人员面临着"何时储备新鲜催化剂"、"何时且如何对催化剂组进行调整"等难题。针对上述问题,课题依托浙江省能源集团有限公司下属燃煤电厂某机组,利用旁路烟气搭建实际烟气脱硝催化剂性能测试平台,利用真实烟气进行催化剂活性检测,使活性检测结果更接近工况真实值;并在分别掌握单层和整体催化剂活性和失活常数的基础上,应用催化剂失活方程及末端活性值,建立重组催化剂组预估使用寿命的计算模型;结合催化剂更新、再生、加装、储运等方面费用进行更换调整经济性评估,得到不同调整方案形成的新催化剂组合单位使用寿命所对应的调整费用;最终经调研并综合考虑所在燃煤机组实际运行情况、单层及整体催化剂实际烟气平台活性检测结果、新催化剂组预估使用寿命及更换调整经济性评估,制定了一套适用于燃煤电厂的脱硝催化剂更换调整策略。该策略已在浙能集团下属多个燃煤电厂应用实施,指导电厂运行、管理人员对脱硝催化剂进行更高效、经济的精准管控,实现对脱硝运行心中有数、对催化剂管理有据可寻,具有广泛的行业推广应用价值。

     

    Abstract: Since all kinds of coal-fired units in China have completed the transformation of ultra-low emission and large areas of denitration catalysts have entered the end of their life, the managers of power plants are faced with problems such as "when to reserve fresh catalysts" and "when and how to adjust the catalyst groups". To solve the above problems, relying on a unit of a coal-fired power plant affiliated to Zhejiang Energy Group Co., Ltd., the project used bypass flue gas to build a test platform for actual flue gas denitration catalyst performance, and used real flue gas to conduct catalyst activity detection, so that the activity detection result was closer to the real value of the working condition. On the basis of the activity and deactivation constants of monolayer and monolayer catalysts, respectively, the deactivation equation and terminal activity value were used to establish the calculation model for predicting the service life of the recombination catalyst group. Combined with the costs of catalyst renewal, regeneration, installation, storage and transportation, the economic evaluation of replacement adjustment was carried out, and the adjustment costs corresponding to the service life of the new catalyst combination unit formed by different adjustment schemes were obtained. Finally, a set of replacement and adjustment strategies for denitrification catalysts suitable for coal-fired power plants was developed after investigation and comprehensive consideration of the actual operation of the coal-fired power unit, the actual activity test results of single layer and monolithic catalyst platform, the estimated service life of the new catalyst group and the economic evaluation of replacement and adjustment. This strategy has been applied and implemented in a number of coal-fired power plants affiliated to Zheneng Group to guide the operation and management personnel of the power plant to carry out more efficient and economical precise control of denitrification catalysts, so as to realize a clear understanding of denitrification operation and evidential management of catalysts, which has a wide range of industry promotion and application value.

     

/

返回文章
返回